Abstract

The main role of 500 kV extra high voltage Gas Insulated Substation in transmission system is serves connection between the electrical generation and transmission system. To improve equipment performance and the quality and reliability of electricity distribution need time to maintain gas insulated line compartment but preparation to maintenance requires a long time, limited maintenance duration and long implementation of gas evacuation. This paper is object to redesign Gas Insulated Switchgear (GIS) to Semi Air Insulated Switchgear (AIS) on 500 kV side and 150 kV side with new design of Gas Insulated Line compartment in order to accelerate maintenance and gas evacuation job. with surveys, observations, analyses and Root Cause Problem Solving (RCPS), it can be seen the initiation of improvement to accelerate the maintenance of IBT and accelerate the repair of anomalies in the gas insulated line. After redesign Gas Insulated Switchgear to Semi Air Insulated Switchgear, this results show maintenance IBT after redesign is 25 hours faster and duration anomaly on GIL after redesign 24 hours faster.

Full Text
Published version (Free)

Talk to us

Join us for a 30 min session where you can share your feedback and ask us any queries you have

Schedule a call