Abstract It is imperative that a completed well be adequately equipped to fully control the flow of any fluid from the well at all times. Regardless of the nature, size or type of equipment that an operator may be running in or out of the wellbore, the procedure must assure that the wellhead, blowout prevention equipment and any other ancillary equipment be capable of providing that control. Two accepted practices are to either fill the wellbore with a fluid of sufficient density to create a hydrostatic head that exceeds or balances the pressure of formation open to the wellbore, or to perform live well servicing. The latter involves snubbing the production tubing or working string into and out of the well under pressure. The snubbing method is used when there is a concern that kill fluids could damage the formation inflow capacity of the well. This case reviews a failure to control a gas well while snubbing out a working string with variable diameter tools being used to retrieve a tubing conveyed perforating gun from a well in Alberta. The well had been perforated, briefly flow tested and was being prepared for a fracture stimulation treatment. Drilling and Initial Completion History A well license was issued on January 23, 1986, for the well, Lac ef al. Minehead 6-18-49-17 to be drilled for the purpose of obtaining production from the Cardium formation at a projected depth of 2440 m. Figure 1 shows the location of the wellsite, approximately 35 km south of the Town of Edson, in west central Alberta. The well was spudded February 4, 1986, and drilled to total depth by March 7, 1986. As shown in Figure 2,139.7 mm casting was run to 2436 m and cemented. A 60.3 m tubing was run in the well and the Cardium Sandstone was perforated from 2385.5 m on March 18, 1986, using a tubing conveyed perforating gun (TCP). A 38 m3 liquid CO2 stimulation squeeze was conducted on March 19, 1986. A modified isochronal backpressure test and final pressure buildup were conducted during the period March 26, 1986 to April 13, 1996. The results indicated limited inflow, an AOF of less than twenty 101 m3/d with some condensate. The shut in sand face pressure was 23,270 kPa. The final tubing pressure was 16,170 kPa and the final casing pressure was 16,690 kPa. Because of the limited flow capacity of the well it was decided that a fracture stimulation treatment was necessary to make the well capable of commercial production. The information presented in this paper up to the section "Well Control Operations" was gathered from interviews and discussions with representatives of the licensee, some contractors, other government agencies and ERCB field staff sent to the site immediately after the initial notification of the blowout. The well control presentation is based on ERCB field staff observations and the authors were on site for the last two days of the well control operation.
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