Changqing oil field generally used sucker rod pump. In 2015, the maintenance operations reached 42 thousand times, the cost is about 550 million RMB, the work caused by tubing and sucker rod lopsided wearing accounts for 42.8% of the total. This paper focused on the main factor of lopsided wearing which caused high frequency of maintenance work, a three-dimensional mechanical simulation model of sucker rod string was established based on the analysis of borehole trajectory, rod mechanics; A model for calculation the neutral point of double material composite pipe and steel tubing is carried out; The calculation method of allowable stress is modified; at the same time, the application conditions of the mature process is standardized, to achieve the integration of technology management. The sucker rod lateral force dynamic distribution and allowable stress calculation method, the sucker rod parameter optimization and real-time warning, optimization of structure and the amount of wear resistant pipe string have been applied in oilfield. Compared with 2015, The number of maintenance operations decreased more than 6000 wells, operation frequency by 0.99 times / year - wells decreased to 0.85 times / year - wells, which is composed of 14 thousand and 500 well tube and rod failure wells decreased to 13 thousand and 300 wells, decreased 8%, annual cost savings of nearly 60 million RMB. It will have important guiding significance to prolong the pump checking period and cost control.
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