Abstract

The well-called KD-2 (for confidential reasons) is not producing because the bottom hole pressure of the well is greater than the reservoir pressure. The purpose of this paper is to activate the well KD-2 by the gas lift and electric submersible pump (ESP) with a rotating gas separator combination in order to increase its production. The completion and the pressure, volume, and temperature (PVT) data are processed under Pipesim and by integrating a certain number of calculations by the nodal analysis and the decline curve methods. The results obtained show that well KD-2 activated by the gas lift provides a flow rate of 3038.019 STB/day. In order to increase the flow rate of well KD-2 activated by the gas lift, the ESP with rotating gas separator is added and the flow rate becomes 4845.325 STB/day which represents a gain of 59.48% in flow rate. In addition, the gas lift and ESP with rotating gas separator combination guarantees an eight-year operating period for a probability of $ 3,601,197 with a return on investment of 2 months. The gas lift and ESP with rotating gas separator gas combination can be used to optimize the production of low-flow wells in the same geographical areas and to consider the reactivation of dead wells.

Full Text
Paper version not known

Talk to us

Join us for a 30 min session where you can share your feedback and ask us any queries you have

Schedule a call

Disclaimer: All third-party content on this website/platform is and will remain the property of their respective owners and is provided on "as is" basis without any warranties, express or implied. Use of third-party content does not indicate any affiliation, sponsorship with or endorsement by them. Any references to third-party content is to identify the corresponding services and shall be considered fair use under The CopyrightLaw.