Meat factory effluent contains fat, protein, diluted blood, and suspended solids. As a result, nutrient and organic concentrations in this effluent are incredibly high, and residues are slightly solubilized, likely to impact environmental pollution on streams, rivers, and other watercourses if discharged untreated. The biodegradation of abattoir waste was studied using a laboratory-scale cylindrical sequencing batch reactor (SBR) in aerobic mode. The aerobic sludge was collected from the aeration compartment of a paper and pulp effluent treatment facility and cultivated in a 2.83-L Perspex-based laboratory SBR. The raw wastewater comprised 6494 ± 2144 mg/l chemical oxygen demand (COD), 1946 ± 607 mg/l biochemical oxygen demand (BOD), 1722 ± 159 mg/l total suspended solids (TSS), 3062 ± 592 mg/l CaCO3 alkalinity, 7.00 ± 0.27 pH. The duration of a complete cycle was 24 h and comprised four phases: fill (5 min), react (23 h 10 min), settle (40 min) and draw (5 min). The whole experiment was divided into four phases and the dilution was done with the help of domestic sewage. In the first stage, the reactor was fed four times diluted slaughterhouse effluent on a 24-h cyclic operation for two weeks. After achieving a significant reduction in COD, the organic content of the input was raised by lowering the dilution factor. In the second and third phases, the reactor was fed three times and twice diluted samples for two weeks each operating at the same cyclic interval. In the final stage, raw effluent was fed to the reactor for two more weeks. The average COD value of diluted wastewater in the first, second, third and fourth phase was 1040 mg/l, 3168 mg/l, 4800 mg/l, and 5200 mg/l, respectively. The COD removal efficiency at the end of the first, second, third and fourth phase was 83%, 93%, 85% and 97%, respectively. The average BOD value of diluted wastewater at the end of the first, second, third and fourth phase was 1120 mg/l, 610 mg/l, 1502 mg/l, and 1350 mg/l, respectively. The BOD removal efficiency at the end of the first, second, third and fourth phase was 84%, 88%, 85% and 98%, respectively. After 8 weeks, at an organic loading rate of 3.06 kg/m3/d, the final phase has achieved BOD and COD removal efficiency of 98% and 97%, respectively. The pH and alkalinity levels were within acceptable ranges. After two months, the sludge's settling characteristics have improved, and the nitrification efficiency of the reactor was roughly 60% at the time of deactivation of the reactor.