ABSTRACTA commercial very high-temperature gas-cooled reactor (VHTR) hydrogen cogeneration system named gas turbine high temperature reactor 300-cogeneration (GTHTR300C) is designed and developed in Japan Atomic Energy Agency (JAEA). Moreover, it has been planned that hydrogen production system and gas turbine system is connect to high-temperature engineering test reactor (HTTR). The reactor system is required to continue a stable and safety operation as well as a stable power supply in the case that thermal-load is fluctuated by the occurrence of abnormal event in the heat utilization system like as the hydrogen production facility. Then, it is necessary to confirm that the thermal-load fluctuation could be absorbed by the reactor system so as to continue the stable and safety operation. The thermal-load fluctuation absorption tests using the HTTR were planned to clarify the absorption characteristics of the HTGR system. However, it is difficult to clarify the phenomenon due to many kinds of fluctuation in nuclear thermal power in the reactor core. Moreover, the actual data regarding how the delay of the temperature response is effective for the reactor system had been gained quantitatively.The thermal-load fluctuation absorption tests without nuclear heating were planned and conducted in JAEA to clarify the absorption characteristic of thermal-load fluctuation mainly by the reactor and by the intermediate heat exchanger (IHX). The absorption characteristics of thermal-load fluctuation can be revealed with sufficient temperature fluctuation. So the tests were conducted with the primary coolant temperature 120 °C which is the start-up temperature of the HTTR. As a result it was revealed that the reactor has the larger absorption capacity of thermal-load fluctuation than the expected one and that the IHX can be contributed to the absorption of the thermal-load fluctuation generated in the heat utilization system in the reactor system. It was confirmed from their results that the reactor and the IHX has effective absorption capacity of the thermal-load fluctuation generated in the heat utilization system. Moreover, the calculation with the safety evaluation code based on RELAP5/MOD3 was performed. It was confirmed that the calculated temperature for the reactor is almost same to the measured one with the new analysis model. On the other hand, it was confirmed that the calculated temperature for the IHX decreased faster than the measured one due to smaller absorption capacity in the calculation model than that in actual one. It can be considered that the calculation for the IHX produces the conservative result. It was summarized that the safety evaluation code can represent the thermal-load fluctuation absorption behavior conservatively.