Abstract

A lot of grout ground leakage occurred during Muduchaideng coal mine separation layer grout work, resulting in serious pollution. To find the mechanism of grout leakage, this paper carried out indoor experiments and on-site measurements. Through the indoor scale model test, the deformation of overburden stratum was captured, which reflected that the horizontal shear band developed at the depths of 289.67–322.48 m, 386.42–431.18 m, and 474.95–524.07 m. Then, these positions were verified through on-site drilling. It was found that the mud slurry consumption increased, the water level dropped, and the borehole wall was seriously deformed in these disturbed positions. Therefore, the reason for this grout leakage was that the overlying separation layer continued to develop upwards, and the borehole was destroyed in the location where the separation layer developed. Then, the grout pipeline was destroyed, and some grout flew towards the ground surface along the pipeline and the borehole wall. This article reveals a kind of grout ground leakage phenomenon in a case study of Muduchaideng coal mine, which can provide a warning for engineering projects.

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