Abstract

The reasons for the occurrence of an impact when closing a butt erfl y valve installed on pipelines that discharge sludge water from horizontal sedimentation tanks of treatment facilities are considered. The assumption about the possibility of water hammer was experimentally refuted. It is hypothesized that the cause of the impact is the disruption of the fl uid fl ow when fl owing around a fl at plate at critical angles of att ack. A numerical experiment was carried out, which consists in modeling the movement of a water fl ow in a completely fi lled, closed space of a pipe. As a result of the experiment, it was revealed that the fl ow stall was caused by the formation of zones of high and low pressure, respectively, before and after the valve. This provides additional energy to increase the closing torque, comparable to the force of a pneumatic actuator, and results in an impact.

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