Abstract

At Zaporozhe Refractory Plant the tunnel kiln of the High-Alumina Part Shop has been converted to firing with natural gas with replacement of the single-passage burners with doublepassage ones equipped with individual supply of primary eold air. Subsequent improvement in the design parameters of the burners and the accomplishment of measures directed toward increasing the effectiveness of combustion of natural gas made it possible to stabilize the thermal operation of the kiln with respect to production of mullite-corundum refractories of the specified quality and reduce fuel consumption by 3%.

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