Abstract

The significant modernization effort in the steel shop at HBIS Group Serbia is the introduction of a Basic Oxygen Furnace, which features bottom stirring with argon and nitrogen, along with the capability for slag splashing with nitrogen through the lance tip after steel tapping from the converter. Implementing this new technology presented a challenge, as it was our first encounter with such advancements. The primary objectives of this modernization were to achieve a lower dissolved oxygen content in steel while reaching the targeted carbon level at the end of the blowing process. This aims to optimize the steel's oxidation degree [%C] [%O], reduce the use of Al as a deoxidizer, increase yield, and achieve a low phosphorus content in steel at the end of blowing. Additionally, it aimed to increase the lining's lifetime through slag splashing and decrease the refractory mass consumption needed for lining repairs. This analysis covers a 7-month period since the start of the campaign with the new refractory lining, based on research conducted on 3,150 heats. Our examination of the process led us to conclude that while certain parameters met our expectations, some results did not reach the anticipated level.

Talk to us

Join us for a 30 min session where you can share your feedback and ask us any queries you have

Schedule a call

Disclaimer: All third-party content on this website/platform is and will remain the property of their respective owners and is provided on "as is" basis without any warranties, express or implied. Use of third-party content does not indicate any affiliation, sponsorship with or endorsement by them. Any references to third-party content is to identify the corresponding services and shall be considered fair use under The CopyrightLaw.