Abstract

This article discusses 6S implementation in Ergonomic Laboratory, Department of Industrial Engineering, Islamic University of Indonesia. This research is improvement project of 5S implementation in Ergonomic laboratory. Referring to the 5S implementation of the previous year, there have been improvements from environmental conditions or a more organized workplace however there is still a lack of safety aspects. There are several safeties problems such as equipment arrangement, potential hazards of room dividers that cause injury several times, placement of fire extinguisher, no evacuation path and assembly point in case of fire, as well as expired hydrant condition and lack of awareness of stakeholders related to safety. Therefore, this study aims to apply the 6S kaizen method to the Ergonomic laboratory to facilitate the work process, reduce waste, improve work safety and improve staff performance. Based on the score 6S assessment increased audit results by 32 points, before implementation is 75 point while after implementation is 107 point. This has implications for better use for mitigate people in laboratory area, save time when looking for tools and materials, safe workplace, as well as improving the culture and spirit of ‘6S’ on staff due to better and safetier working environment.

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