The paper presents findings of the failure analysis of a control rod that resulted in accident to a helicopter during a routine flight. The helicopter crashed due to several events that led to loss of control. Post-accident wreckage examination showed that failure in the non-rotating control rod connecting the swash plate and bell crank was the primary component that led to the accident. The control rod was manufactured from Ti-6Al-4V alloy. Fractography studies revealed that the control rod failed by fatigue mechanism. The fatigue crack initiated at the rod-to-eye-end transition fillet. Fatigue crack initiation was associated with presence of deep machining marks on the fillet surface. After initiation at the machining marks, the crack propagated through the thickness as well as along the machining mark over a length on either side of the crack origin. Study revealed presence of multiple fatigue cracks on the machining marks on the fillet surface. Analysis showed that the primary cause of the fatigue failure of the non-rotating control rod was the stress concentration effect arising from the deep machining marks at vulnerable location, which is the rod–to–eye transition fillet surface. Issues related to the fitment of the bearing in the control rod led to fretting on the inner bearing surface, and this damage contributed to the initiation of the fatigue cracks.
Read full abstract