Abstract

This paper addresses the decay of rotor wake vorticity for a rotor/stator axial compressor, with the axial gap between blade rows being 10, 20 and 30 percent chord, and at both design and high loading levels. Experiments were conducted in a large-scale, low-speed axial compressor. Navier-Stokes calculations were also executed. Both data and Navier-Stokes results reveal that the decay of rotor wake vorticity increases substantially as the axial gap decreases; the decay for 10 percent gap is about twice that of 30 percent. Increased time-mean blade loading causes the vorticity decay to also increase, with this effect more pronounced for large axial gap than small. At the stator inlet mid-pitch location, the wake maximum vorticity for 10 and 30 percent chord gap cases being nearly the same (differ by 3.8%) at design loading. The corresponding stator unsteady force agrees within 5.2%. Variation of vorticity decay with axial gap is directly linked to the change in potential disturbance by the downstream stator on the rotor wake due to the change in gap spacing. This suggests that the stator potential disturbance causes the upstream rotor wake to decay at an increased rate which, in turns, results in a lowered level of stator response compared to that without this stator/wake interaction effect. Thus, in this context, blade row interaction is considered beneficial.

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