Abstract

ABSTRACT Service level adjustments are essential to keep measurement and verification project baselines “updated” with the actual service level that a system provides. In the case of a DSM load shift project on a mine pumping system, it is standard procedure to use a service level adjustment based on daily kWh neutrality. The case study discussed in this article showed that the project achieved impacts in the order of 12.9 MW when the baseline was adjusted in this manner. This approach, however, rested on the assumption that system efficiencies remained unchanged since the DSM intervention was only supposed to shift the system load to other time-of-use periods outside the evening peak period. However, it was found that system efficiency did change by almost 13 percent in this project's case. A service level adjustment approach was consequently required that linked the baseline energy use to the actual service level of the system, which was the daily volume of water pumped out of the mine. The utilization ...

Talk to us

Join us for a 30 min session where you can share your feedback and ask us any queries you have

Schedule a call

Disclaimer: All third-party content on this website/platform is and will remain the property of their respective owners and is provided on "as is" basis without any warranties, express or implied. Use of third-party content does not indicate any affiliation, sponsorship with or endorsement by them. Any references to third-party content is to identify the corresponding services and shall be considered fair use under The CopyrightLaw.