Abstract
Steam gasification kinetics studies were conducted in a modified drop tube fixed bed reactor to approximate the injection of ambient temperature coal into a fluidized bed gasifier. Product gases were measured using a customized rapid response gas analysis system with a quadrupole mass spectrometer. Experiments were done within Regime I temperature range (no mass transfer restrictions), and effects of temperature and pressure on surface chemical reaction were analyzed using three different particle size ranges. The random pore model closely fits the experimental results and the fitting parameters are listed. Char characterizations are presented, including surface area measurements and scanning electron microscope images. Mass transfer resistances were analyzed by comparing experimental and theoretically predicted effectiveness factors using the Thiele modulus, based on particle sizes, temperature, total pressure, and steam partial pressure.
Talk to us
Join us for a 30 min session where you can share your feedback and ask us any queries you have
Disclaimer: All third-party content on this website/platform is and will remain the property of their respective owners and is provided on "as is" basis without any warranties, express or implied. Use of third-party content does not indicate any affiliation, sponsorship with or endorsement by them. Any references to third-party content is to identify the corresponding services and shall be considered fair use under The CopyrightLaw.