Abstract

• Model based simulation is carried out for industrial scale natural drought cabin furnace. • Aspen Hysys and exchanger design rigorous (EDR) program used for modelling and simulation. • Sensitivity analysis was carried out to predict the impact of several parameters on the furnace efficiency. • The study shows potential of significant savings in energy, operational cost and carbon footprint. In all industrial petrochemical plants and refineries, the furnace is the source of heat resulting from fuel combustion with air. The model-based furnace simulation is considered one of the efficient methods help to reduce the energy loss and maintain fixed refinery revenues, conserving energy, and finally reducing external fuel consumption and total fuel cost. In this paper, a model-based simulation is carried out for a natural air draught industrial scale furnace related to Liquified Petroleum Gas (LPG) production plant in Libya to thoroughly investigate the most responsible factors in lowering the furnace butane exit temperature, which is supposed to be two degrees Fahrenheit higher than inlet temperature. Therefore, to resolve this industrial problem, Aspen Hysys V10, coupling with EDR (exchanger design and rating) is used to carry out rigorous model-based simulation. This is specifically used to assess the impact of heat loss from inside the firebox to the surrounding medium and heat loss from the furnace stack and walls, besides the effect of excess air on the furnace efficiency. Furthermore, this research intends to verify whether the operating conditions, such as furnace tubes inlet flow rate, temperature and pumping pressure, are conforming to the upstream process design specifications or need to be adjusted. The results confirm that increasing furnace outlet temperature two degrees Fahrenheit from off specification 190 °F instead of 184 °F is successfully achieved by decreasing upstream stream flowrate 25% below the operating value and cutback excess air gradually until 20%. Also, the results clarify the necessity of increasing the flue gas temperature by 7% over design condition, to gain a significant reduction of heat loss of 31.6% and reach as low as 35.5 MBtu/hr. This improvement is achieved using optimum operating conditions of an excess air of 20%, and flue gas oxygen content of 3.3% delivered to stack. Accordingly, the furnace efficiency has been increased by 18% to hit 58.9%. Furthermore, the heat loss from the furnace walls can be also reduced by 68% from 5.41 MBtu/hr to 1.7 MBtu/hr by increasing the refractory wall thickness to 6 in., which entails an increase in the furnace efficiency by 3.66% to reach 58.96%. Decreasing the heat loss fraction through the refractory wall, pip doors, expansion windows and refractory hair cracks would also increase the efficiency by 21% to reach a high of 59.7%. Accordingly, a significant reduction in daily fuel consumption is observed, which costs 1.7 M$ per year. The outcomes of this research clearly show the potential of reducing the operation and maintenance costs significantly.

Full Text
Published version (Free)

Talk to us

Join us for a 30 min session where you can share your feedback and ask us any queries you have

Schedule a call