Abstract
The Salt Valve and Instrumentation Test was done to provide data on equipment performance in high temperature environments similar to that expected in the next large scale application of that technology. The experiment tested three different valves: (1) a valve with the standard valve body and standard high temperature self-packing material; (2) a valve with the standard valve body and stainless steel O-rings; and (3) a magnetic valve that uses a high temperature coil and no packing material. The first valve, which was used at Solar Two, performed sufficiently throughout the test with only a small leak from the split-body, not the packing material, on the 6th day of testing on the long-term test. The second valve, with the stainless steel O-rings, developed a small leak on the last run of the third test at the bonnet (packing material), at which point it was noted to watch if it got worse and the test continued. By the 6th day of the long-term test, the leak was significant (up to 3 cups per day) and the test was terminated. The magnetic valve failed when exposed to a relatively low temperature of 500 F. According to the manufacturer, it was expected to survive up to temperatures of 600 F. Two different pressure transducers were tested and compared, Taylor and Dynisco. The Taylor pressure transducer was used and proven successful at Solar Two. However, they are no longer made. Therefore the experiment tested a new pressure transducer from Dynisco and compared the results to that of the Taylor. The Dynisco pressure transducer performed inaccurately from the beginning. The pressure transducer was affected by an increase in temperature when the pressure remained the same. Dynisco agreed to recalibrate the pressure transducer and/or send us a new one if the piece was faulty. However, in the process of removing the piece from the system, due to the high temperatures used, the piece had gulled with the stainless-steel piping and broke. Flared fittings versus Swagelock fittings were tested in the experiment as well. Both fittings showed no signs of any leakage when exposed to the high temperatures and corrosive environment. The existing test set-up for the Nagle Long Shafted Pump was used in this experiment and additional test hours were obtained on the pump bearings. However, only 132 hours (5 1/2 days) of the 5000 hours (208 days) were performed due to a salt leak, which required removal of insulation. The experiment had to be terminated prior to removal of the insulation.
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