Abstract

The article deals with a root cause analysis of coining tool failure after its untimely discarding and the design to extend its service life by innovating the manufacturing process. The analysis was performed on the coining die which had to be put out of service due to the insufficient quality of minted stainless coins. The purity of steel and the microstructure of the material of the semi-finished goods were evaluated. Furthermore, an analysis of the coining die failure under the surface and in the core was performed as well as the state of the chromium layer failure on the coining die relief. Based on the results of the analysis, a new experimental coining die was designed and produced according to an innovative manufacturing process. The pressing of the relief was carried out in a vacuum furnace and relief was coated with a TiAlN by the PVD method. New processes introduced in the production of coining die prevented the failure of die punches, extended the time of operation, thereby increasing quality of the coin production.

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