Abstract

A former natural gas processing station is impacted with total petroleum hydrocarbons (TPH) and benzene. Remedial process optimization (RPO) was conducted to evaluate the effectiveness of the historical air sparging/soil vapor extraction (AS/SVE) system and the current groundwater extraction and treatment system. The RPO indicated that both remedial activities offered no further benefit in meeting remediation goals. Instead, an in situ chemical oxidation (ISCO) system was recommended. Ozone was selected, and the results of a bench test indicated that the ozone demand was 8 to 12 mg ozone/mg TPH and that secondary by-products would include hexavalent chromium and bromate. A capture zone analysis was conducted through groundwater flow modeling (MODFLOW) to ensure containment of the injected oxidant using the existing groundwater extraction system. Results of a pilot study indicated that the optimum frequency of ozone sparging is 60 minutes in order to reach a maximum radius of influence of 20 feet. TPH concentrations within the treatment zone decreased by 97 percent over two months of ozone sparging. Concentrations of hexavalent chromium and bromate increased from nondetect to 44 and 110 mg/L, respectively, during the ozone sparging but attenuated to nondetectable concentrations within three months of system shut down. ©2016 Wiley Periodicals, Inc.

Full Text
Paper version not known

Talk to us

Join us for a 30 min session where you can share your feedback and ask us any queries you have

Schedule a call

Disclaimer: All third-party content on this website/platform is and will remain the property of their respective owners and is provided on "as is" basis without any warranties, express or implied. Use of third-party content does not indicate any affiliation, sponsorship with or endorsement by them. Any references to third-party content is to identify the corresponding services and shall be considered fair use under The CopyrightLaw.