Abstract
The paper presents the modelling, simulation and analysis of the transient behaviour of a 340 MW pump-turbine in case of emergency shutdown in generation mode with particular attention to the possible draft tube water column separation. First, the model of a pumped storage power plant with simplified layout is setup with the EPFL software SIMSEN. This model includes a penstock feeding one 340 MW pump-turbine with the related rotating inertia and a tailrace tunnel. The model of the tailrace tunnel allows for water column separation simulation. Thus, the related SIMSEN model is introduced and validations are briefly presented. Then, the influence of the tailrace tunnel length and diameter on the minimum pressure in the draft tube is investigated through a parametric study first without water column separation model. Finally, the simulation results of the transient behaviour of the pump-turbine with downstream water column separation are presented for different degree of severity triggered by the submergence and the tailrace tunnel dimensions taken as parameters.
Talk to us
Join us for a 30 min session where you can share your feedback and ask us any queries you have
Disclaimer: All third-party content on this website/platform is and will remain the property of their respective owners and is provided on "as is" basis without any warranties, express or implied. Use of third-party content does not indicate any affiliation, sponsorship with or endorsement by them. Any references to third-party content is to identify the corresponding services and shall be considered fair use under The CopyrightLaw.