Abstract

Abstract Block H, located in 1,300 meters of water depth at offshore Sabah, consists of Rotan and Buluh fields. The subsea trees, jumpers, manifold, umbilicals, risers and flowlines were installed and tied-back to an FLNG facility. The objective of this project was to develop most practical and effective solutions to overcome flow assurance challenges owing to low seabed temperature and high-pressure gas to achieve 1st gas from the first deepwater gas field in Malaysia. A model was built in OLGA software with all field conditions to run simulations and predict process parameters at every critical point in subsea wells, risers and flowlines as well as topside facilities. Besides, all constraints from the subsea wells, jumpers, risers and flowlines all the way to topside inlet receiving facilities were carefully reviewed and optimized with an abundance of caution to determine the stepwise approach by utilizing the high-pressure gas from wells to remove around 1,000 m3 of pre-filled MEG fluid out of the flowline, called ‘DeMEG operation’ before feeding gas to LNG process operations. With 200-230 barg pressures from deepwater gas wells and 2-4°C temperature at seabed as well as pre-existing water content in saturated gas given by reservoir aquifer, this start-up operation would expect to be in the hydrate zone. One of the unavoidable potential consequences was a hydrate formation and could result in plugging of jumpers, risers or even flowlines. The DeMEG operation results indicated the lowest temperature at the downstream of the subsea choke was −23°C due to Joule-Thompson cooling during the cold start. One mitigation strategy was to inject a batch of MeOH at the subsea wellhead until the temperature is above the hydrate point. After the gas flowed along the flowlines, it would cool down to the seabed temperature during the steady state condition. Hence, additional mitigation was to continuously inject Mono Ethylene Glycol (MEG) as another thermodynamic hydrate inhibitor mixed with gas stream. The MEG affixed water molecules and thus deterred them from forming a cage around gas molecules to prevent hydrate formation. A multi-stage DeMEG operation was carefully planned to overcome liquid handling capacity at topside and eventually executed at offshore until the remaining MEG in the flowline was as low as reasonably practical to proceed with gas production from the field. With an excellent collaboration from the team and proper planning, the DeMEG solution together with hydrate mitigation strategy were proven to be effective and the commissioning operation was successfully completed as per the plan until the 1st gas was achieved on 6-Feb-21 and supplied to FLNG. The 1st LNG drop subsequently came in 7 days later. This field has increased production volume around 270MMSCFD, equivalent to 45,000 barrels of oil per day to PTTEP and JV partners.

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