Abstract

Power generating unit no. 4 of Troitskaya State District Power Plant (SDPP) is incapable of operating with a nominal load of 278 MW because of high aerodynamic drag of the gas path. At present, the maximum load of the two-boiler single-turbine unit is 210 MW practically without a possibility of adjustment. The results of numerical simulation of the gas flow for the existing gas path from the electrostatic precipitator (EP) to the smoke exhausts (SEs) and two flue designs proposed for renovation of this section are presented. The results of simulation show that the existing flue section has high aerodynamic drag, which is explained by poor, as regards aerodynamics, design. The local loss coefficient, in terms of the dynamic pressure in the sucker pocket of the smoke exhaust is equal to 4.57. The local aerodynamic loss coefficient after renovation at the considered section according to the first version would make 1.48, and according to the second version 1.325, which would reduce losses at this section by more than a factor of three, and ensure the power unit operation with the rated load.

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