Abstract

Nowadays, applying anammox to treat high nitrogenous side-stream wastewater has taken a step forward. However, the partial nitritation process is sensitive to the ammonium concentration and the nitrogen loading rate, which significantly influences the nitrogen removal performance. This study investigated the performance of a novel nitritation pilot-scale reactor which was divided into four chambers. The nitrite accumulation efficiency reached more than 90 % in the rural wastewater treatment process. As the reactor was divided into four chambers, the comprehensive statistical results showed that the concentration of free ammonium in the front chambers had been effectively improved. The proportion of free ammonium concentration (>0.1 mg NH3·L−1), which could inhibit the activity of nitrite oxidizing bacteria, in first chamber (PN1) was 2 times higher than in the last chamber (PN4). Meanwhile, Nitrosomonas, responsible for ammonium oxidation to nitrite, was highly enriched in the first two chambers even though the dissolved oxygen was maintained at 1.5 ± 0.3 mg·L−1. Compare to conventional reactor, the resistance of the novel reactor to volumetric shock loading has been enhanced. Even though the ammonium loading rate fluctuated greatly, the effluent was still stable and could meet the demand following the anammox process. This study demonstrated that the reactor with multi-chambers could effectively improve the nitrite accumulation efficiency in the partial nitritation process and thus provide a new perspective on the partial nitritation process in a single reactor and further promote the anammox performance in the wastewater treatment process.

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