Abstract

Abstract Exhaust stack liners of a test rig for gas turbine burners failed locally by ruptured fasteners and fallen-off liner plates. Misalignment of the plating relative to each other and relative to their fasteners caused restraint of the expanding and shrinking liner plates upon start-up and shutdown of the burner rig. The fastening holes of the failed liner plates were not concentric, but misaligned relative to each other and relative to their fastener bolts. This exerted a shear loading on the threads of the fastening bolts, which in turn caused a mean stress shift and damaged the threads of the fasteners by nicking. So pre-loaded, the fastening bolts were not able to withstand the vibratory loads from the flowing exhaust gases and failed due to fatigue.

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