Abstract

ABSTRACT A laboratory study was conducted at simulated in-situ geothermal conditions to identify the mechanisms responsible for significant declines in permeability. Testing was conducted on core material retrieved from Well 78-30 in the East Mesa KGRA, Imperial Valley, California. In this paper, apparatus, procedures and results are described. Damage in this formation, which was not originally thought to be water sensitive, is attributed to cation exchange and the removal processes which alter the stability of the clay structures. Fluid shearing dislodges particles, which clog pore throats and irreversibly reduce permeability. The implications of these findings on operating procedures and production of the well can be significant and are discussed.

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