Abstract

Abstract An important noise source in modern high bypass ratio turbofans is from multiple pure tones produced by the fan during takeoff. An experiment conducted on a 1.5 pressure ratio fan in an internal flow facility provided dynamic pressure measurements to investigate multiple pure tone generation and propagation. Since multiple pure tones are generated by blade shock variation primarily due to the fan’s blade stagger angle differences, the blade stagger angles were measured with an array of over-the-rotor dynamic pressure transducers. Multiple pure tone measurements were made with 30 wall-mounted dynamic pressure transducers from 0.4 to 1.1 diameters upstream of the rotor. Measured blade stagger angle differences correspond to the the shock amplitude variation measured upstream. The acoustic field was extracted from the dynamic pressure signals using principal component analysis as well as duct mode beamforming. Shocks traveling out the inlet were found to couple to duct modes propagating at similar angles. Over-the-rotor acoustic liners appear to reduce rotor shock variation resulting in a reduction of sub-harmonic multiple pure tone sound pressure levels by 3–4 dB.

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