Abstract

This research addresses the problem of leveling workloads in a multi-product final assembly area. In which it was found that 27.4% of the time is used for set up and the current distribution presents areas of opportunity. The target was to implement improvement actions to make use of resources more efficient in the production process in the aforementioned area through Lean Manufacturing tools. The results obtained consist of eight products generated with the support of lean manufacturing support tools such as SMED, Workload Balancing and MUDA waste identification, achieving important results among which productivity in the area stands out from 109% to 125%, as well as a reduction in set-up time from 17 min to 4.4 min.

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