Abstract

This paper presents a case study of a rotor fault occurring in the rotor generator of a steam power plant located in Lontar, Banten Province, Indonesia. The steam power plant has 3 x 315 MV capacity and uses hydrogen in the cooling system. The issue arising during the operation was caused by heat transfer exceeding the normal level. The grounding of the rotor occurred through rising vibration and temperature, tripping the generator unit. During repairs, the axial spacer was replaced with a new model, where it is longer than the original, adding a bar spacer at a previously unavailable position and creating a cooling track profile. This is a case study on the replacement of the axial spacer model aimed at preventing the expansion of the winding, so as not to touch with each other, through the installation of a longer axial spacer and the addition of the spacer bar, and lastly adding the track profile to the cooling hydrogen gas flow thereby maximizing the cooling process from the end winding rotor generator. Heat transfer is an analysed parameter related to the model change of the axial spacer. The addition of a track cooling gas flow has been able to maximize the heat transfer process, which is simulated in this paper. The performance of the rotor generator increased through several parameters after the replacement of the axial spacer model.

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