Abstract

Smooth and notched specimens of a 319 cast aluminium alloy were fatigue tested under a Society of Automotive Engineers service load history in the as‐cast and hipped conditions. The hipping process, which includes subjecting the cast material to a high pressure at high temperature and then slowly cooling down to eliminate internal flaws, decreased the flaw size and improved the fatigue life of cast Al 319 smooth specimens. A 0.6‐mm‐diameter hole was drilled at the notch root of notched specimens to simulate a natural flaw at the notch root. Specimens with two different notch sizes were tested. Circular edge notches reduced the fatigue strength and a 0.6‐mm‐diameter drilled hole at the notch root resulted in a further reduction.The fatigue lives of smooth specimens, notched specimens and notched specimens with a flaw at the notch root subjected to the service load history were predicted using the strain‐life approach, an effective strain‐life approach and a strain‐based intensity factor crack growth model. In crack growth modelling of the fatigue life of smooth cast aluminium specimens the flaw was modelled as a circular edge notch having the same diameter as the flaw. However, in the case of a flaw at a notch root the flaw was modelled as a three‐dimensional cavity subjected to the notch stress field and the crack length was predicted in the longitudinal and transverse directions of the specimen cross‐section. The strain‐life approach was unconservative for all specimen geometries studied. The effective strain‐life approach gave good predictions for smooth and blunt notched specimens but gave very conservative predictions for the specimens with flaws in the notch roots. The crack growth calculations gave accurate predictions for all the specimen geometries.

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