Abstract

The lifting lug is one of the most important structures of aerial bomb, which mainly bears the variable amplitude cyclic loading during the working process. In this paper, the failure analysis of several lifting lugs which failed in fatigue test was carried out. Firstly, through the mechanical analysis, fatigue cumulative damage analysis and fracture surface analysis of the lifting lug structure, it was determined that the fracture failure was not caused by the issue of structural design, but by the Al2O3 inclusion defect in the casting process. Next, the crack source defect was equivalent to the initial crack, and the fatigue full-life was predicted by the method of fatigue crack growth (FCG). The FCG process was divided into two stages: small crack growth stage and long crack growth stage for life prediction respectively. Finally, the validity of this method was verified by comparing with the experimental results, and it was suggested to adopt advanced lifting lug casting and detection technology to prevent similar faults.

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