Abstract

This study investigated the effects of clogging in Pervious Concrete (PC) from January 2015 to December 2022. Three different PC mixtures were used, which included coarse aggregate (4.75-9.5 mm), fine aggregate (0-20% weight of coarse aggregate), cement (340 kg/m3), and w/c ratio of 0.35. The samples were tested for compressive strength, permeability, and porosity. The best PC mixture containing 10% fine aggregate was selected for monitoring clogging over time. This mixture had a compressive strength of 24.7 MPa, permeability of 1.19 mm/s, and void content of 13.96%. A large-scale prototype of PC10 (10% of fine aggregate) measuring 3.5 m in length, 1.7 m in width, and 0.20 m in depth was constructed in Mashhad City, Iran. The in-place infiltration rate was measured on a monthly basis as the PC experienced different rainfall levels. The results showed that due to clogging, the infiltration rate was reduced by an average of 10% for the first four years of the experiments. This was followed by a substantial reduction of 20% in 2019 and 16.75% in 2020. Due to a high level of clogging, the infiltration rate was reduced by 5.02% and 2.23% in 2021 and 2022, respectively. However, the system still has the capacity to infiltrate at 1.14 mm/s. Although no maintenance was performed on the PC system, its efficiency and lifespan were substantially reduced. Nonetheless, the system can still be considered as an effective solution for stormwater management.

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