Abstract

The elevated tanks are considered as very sensitive structures in seismic movement condition. Moreover, the conical steel tank manufacturing without local geometric imperfection seems to be too difficult. In generally, the latter is the most responsible factor to define the shell structures buckling capacity. For this reason, several theoretical and experimental researchers studied the performance of this type of structure under seismic loading. The present study aims to demonstrate the local geometric imperfection effect on dynamic buckling of elevated water tank. Using the three dimensions finite element technique to study the seismic response of perfect and imperfect elevated water tank was established taking into account the following factors; the interaction fluid structure (FSI), the wall flexibility, the local geometric imperfection, the nonlinear time history analysis, the material and geometric nonlinearity, and this by the application of three different instability criteria for the critical PGA estimate. The critical PGA of the imperfect elevated water tank numerical models decreased by 45, 45% compared to the elevated water tank numerical model without local geometric imperfection. The obtained results confirm the local geometric imperfection effect on dynamic buckling of elevated water tanks.

Highlights

  • Many researchers have studied the dynamic behaviour of elevated tank

  • An efficient 3D finite element analysis method was used to evaluate the dynamic behaviour of elevated tanks

  • In the third part in order to clearly show the local geometric imperfection effect on the dynamic response of the elevated tanks, the PGAcr of elevated tank is calculated for imperfect model and the obtained results are compared to the perfect model Figure 3

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Summary

Introduction

They are generally used as water storage in our daily lives and as well as hydrocarbon storage in the industry field. The water tanks are generally installed on steel or reinforced concrete tower supports to avoid the use of pumping installations. Several tanks have been severely damaged and some have collapsed with disastrous results. The severe damage sustained during the earthquake, namely; Alaska 1964, Niigata 1964, Parkfield 1966, San Fernando 197, Imperial County 1979, Northridge 1994 and Asnam 1980. Many researchers have studied the dynamic behaviour of elevated tank. Housner (1963) has allowed practicing engineers to perform the seismic responses analysis of the elevated rigid tanks by using the two-mass method. The liquid was assumed to be incompressible and non-viscous. The model has been adopted in many codes [1]

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