Abstract

The paper presents results of research and failure analysis undertaken to determine failure causes of a steam turbine casing. After 130,000 hours of service the crack in a outer shell of the turbine casing was found. The inner shell of the casing was made of cast steel grade G21CrMoV5-7, and the outer shell of grade G20CrMo4-5. Following research were performed in order to determine causes of the casing failure: chemical analysis; microstructure examinations with the use of light microscope, scanning electron microscope (SEM); mechanical properties examinations using the Charpy impact test, and Vickers hardness test; fracture mode evaluation with SEM.

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