Abstract

Since recessed channel array transistor (RCAT) was adopted from 100 nm feature size, gate-induced-drain-leakage (GIDL) has been the major cause of refresh fail. [1] The process of inner-gate-recess was adapted and GIDL in RCAT structure has been remarkably reduced by lowering electric field at overlap region. Fig.1 (a) and (b) show the VSEM image of inner-gate-recessed-RCAT and the electric field simulation, respectively. The process of recessing gate-poly was executed at both cell array transistor such as RCAT and planar transistor in logical circuits. In case of planar transistor, there was no need to recess poly-Si except SiO2 layer. During the etching of poly-Si in the cell array, the thin oxide layer in the planar area should be preserved to prevent Si-pitting. HBr/O2 plasma has been used to improve the selectivity of poly-Si to gate oxide in gate-stack etching. HBr/O2 plasma produced polymer residues such as SiBr and SiBrOx layer on the underlying gate oxide and polymer residues should be removed. [2, 3] Fig.2 shows the variation of stand-by current of DRAM and propagation time of inverter (tPD) with wafer number in a lot investigated. Wafer number indicates the order in processing. As the number of wafer increased, stand-by current increased and tPD decreased. Fig.3 shows the saturation current of PMOS and the saturation current also decreased with increasing wafer number. Structural analysis was evaluated, and the difference between the first wafer and the last wafer was found. There was thicker SiO2 layer on the gate stack in the first wafer. Especially, to make the gate recessed profile of RCAT, the over-etch time increased and the exposure time in HBr/O2 plasma also increased. It induced to increase polymer residues and unexpected SiO2 offset spacer. As the HF removal was delayed for measuring critical dimension (CD) of gate stack and thickness of remain substrate, deposited SiBr among the polymer residues reacted with O2 in the air and additional SiO2 was grown. [4] The first wafer in the lot investigated had much more delay time than the last wafer. Therefore thicker SiO2 in the first wafer was grown than that of the last wafer, and the SiO2 in the first wafer was insufficiently removed by HF clean. SiO2 offset made under-lap from gate to source/drain and induced increasing resistance and decreasing saturation current. [5, 6] Fig.4 (a) and (b) show the TEM profiles and explain the cause of saturation current difference obtained from the same lot. Immediate HF cleaning after gate etching was introduced and CD was measured with increasing time by the scanning electron microscope (SEM). Fig. 5 shows the CD variation monitored as a function of delay time. While SiO2 layer was steadily grown with increasing delay time without HF cleaning, the SiO2 and residual SiBr layer on the sidewall of gate stack were easily removed and additional SiO2was not grown in case of immediate HF clean. As the integration process is more complicated and delicate, small variation brings the big failure. Delay time after reactive ion etching should be reduced, and immediate cleaning should be appropriately considered.

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