Abstract
Research was conducted on pilot-scale, two-stage batch-flow constructed wetland systems for domestic wastewater treatment. Synthetic domestic wastewater was treated in a pre-acidification reactor with a hydraulic retention time (HRT) of 3 hours and the average removal rate of chemical oxygen demand (COD) and ammonia-nitrogen (NH4-N) reached 30% and 13.6%, respectively. The first-stage constructed wetland operated with up-flow and batch feed and drain. One cycle was 12h, including 6h feed and 6h drain. With HRT of 3 days, the effluent COD concentrations fluctuated from 32.5 mg/L to 103.4 mg/L, removal rates varied from 60% to 88%; effluent NH4-N concentrations were in the range of 4.8 mg/L to 10.8 mg/L, removal rates varied from 50% to 70%. The second-stage constructed wetland operated with down-flow, which one cycle was 24h, including 12h feed and 12h drain. With HRT of 1 day, effluent COD concentrations varied from 15.7 mg/L to 48.7 mg/L, removal averaged 53.2%; effluent NH4-N concentrations ranged from 0 mg/L to 0.4 mg/L, average removal exceeded 99%. The spatial variation of COD and NH4-N in the first-stage constructed wetland demonstrated that entrainment of air during draining of constructed wetland could strengthen the removal of COD and NH4-N. Temperature had no significant effect on COD degradation while obviously affected the removal of NH4-N.
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