Abstract

This work reports observations of a tokamak plasma that experienced a thermal quench due to a large, transient high-Z influx but avoided a current quench. This is argued to be caused by the presence of lower hybrid range of frequency (LHRF) waves that sustain a non-thermal, current-carrying electron population. In Alcator C-Mod L-mode plasmas at kA, m−3, nearly all of the current can be sustained non-inductively by injecting 700 kW of LHRF power at 4.6 GHz and . A sudden influx of a large amount of tungsten, , triggers a cooling wave that propagates at 2–3 m s−1 all the way into the core, dropping on-axis Te from 3 keV to temperatures less than measurement floor of 50 eV. An off-axis reheat begins after 100 ms, but Te profiles remain hollow for 300–350 ms after the injection. Throughout this temperature evolution, the plasma density, current and shape remain unchanged to within 10%. Following the expulsion of the tungsten, the plasma returns to its baseline conditions and the plasma ends as planned with a controlled current ramp-down. Energy balance analysis shows the LHRF power continues to be absorbed in the plasma after the thermal quench, as a significant fraction of it is needed to be consistent with radiated power measurements. Examination of current relaxation time, , and fast-electron slowing down time, , indicate the LHRF must contribute to driving current, despite the low temperatures, as the current remains nominally stationary despite ms and ms for relativistic electrons. These measurements represent an important existence proof of a possible technique for avoidance of disruptions caused by sudden, unplanned influx of impurities in the form of dust or flakes of high-Z wall material. Implications and suggestions for future experimental and modeling and simulation work are summarized.

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