Abstract

During a shaft and associated sprayed concrete lining (SCL) tunnel construction in a new line of Guangzhou Metro, site monitoring recorded ground surface settlement was much larger than that predicted in the design. This raised the alarm to the safety of an adjacent high-pressure gas pipe. Close-form and analytical calculations and non-coupled and coupled numerical analyses were carried out to back analyze the settlement. It was found the primary contributing factor to the excessive ground settlement is water loss-induced ground consolidation, which is commonly encountered during underground construction in south China where complex strata, such as granite residual soil and fully weathered granite, are present. This paper details the back analysis process and discusses mitigation measures that should be adopted for construction in similar ground in the future.

Full Text
Paper version not known

Talk to us

Join us for a 30 min session where you can share your feedback and ask us any queries you have

Schedule a call

Disclaimer: All third-party content on this website/platform is and will remain the property of their respective owners and is provided on "as is" basis without any warranties, express or implied. Use of third-party content does not indicate any affiliation, sponsorship with or endorsement by them. Any references to third-party content is to identify the corresponding services and shall be considered fair use under The CopyrightLaw.